REPAIR OF KARUMBU VOLTAGE USING THE METHOD BREAKING LOAD AT PT. PLN (PERSERO) ULP WOHA

Authors

  • YASYFIN NUR MUHAMMAD YASYFIN
  • Indra Darmawan Universitas Teknologi Sumbawa
  • Titi Andriani Universitas Teknologi Sumbawa
  • Muhammad Hidayatullah Universitas Teknologi Sumbawa

DOI:

https://doi.org/10.51401/altron.v2i02.2177

Keywords:

Feeder Load Break, Voltage Rectification, Voltage Drop, ETAP 12.6.0

Abstract

The electrical energy that is distributed to customers is connected to the distribution network. Within the scope of the electricity distribution network, there are problems, namely the rating capacity that exceeds the feeder load and the length of the network on the feeder. This is dangerous because the load being served is too far away, and the excessive load will increase the current flowing through the conductor. so that it causes the voltage to drop to the customer, and if there is a feeder disturbance, it will expand the blackout area. Power loss is a problem that has always been faced by PT. PLN (Persero) and is unavoidable. This is also similar to the conditions that occurred at PT. PLN (Persero) ULP Woha, where the load on the Karumbu feeder is too heavy with a capacity of up to 91 amperes and a feeder length of 167 kMs. One of the solutions offered is the need to solve the feeder and plan for the construction of the Monta switch substation to reduce the load and length of the Karumbu feeder by simulating using ETAP 12.6.0 software. Based on the simulation results using the ETAP 12.6.0 software, the voltage at the end of the Karumbu feeder was obtained from 18.087 kV to 18.885 kV after solving the feeder load. The benefits that will be obtained later are reducing the burden on the Karumbu feeder and improving the voltage on the 20 kV and customer sides.

References

B. Winardi, A. Warsito, and M. R. Kartika. 2015. "Analisa Perbaikan Susut Teknis dan Susut Tegangan pada Penyulang KLS 06 Di GI Kalisari dengan Menggunakan Software ETAP 7.5.0," Transmisi : Jurnal Ilmiah Teknik Elektro, vol. 17, no. 3, pp. 135-140.

D. Marsudi, 2006, “Operasi Sistem Tenaga Listrik Edisi Kedua”, Yogyakarta : Graha Ilmu.

PT. PLN (Persero).“Spesifikasi desain untuk JTM dan JTR. SPLN 72:1987”.

Aqif, Abrar, dan Zulfahri. 2019. “Analisis Pemindahan Beban Penyulang Perawang Gardu Induk Garuda Sakti Guna Meningkatkan Kinerja Sistem Kelistrikan”. Universitas Lancang Kuning.

Danu, Rudy, dan Fardhan. 2017. “Analisis Pemecahan Beban Penyulang Anoa di Muntok Dengan Menggunakan Simulasi ETAP 12.6.0”. Universitas Bangka Belitung.

Ilham, Yasin, dan Ade. 2018. “Kajian Kelayakan Operasi Pecah Beban Penyulang Beta (SJ-2) Untuk Kehandalan Sistem Kelistrikan Kota Bitung”. Universitas Negeri Gorontalo.

Wahyu, Asmar, dan Hendrawan. 2017. “Analisa Pecah Beban Penyulang KB5 Di PLN Rayon Koba Untuk Perbaikan Tegangan Dan Susut”. Universitas Bangka Belitung.

Rifal, Sukarno, dan Haddin. 2019. “Analisis Perhitungan Rugi-Rugi Daya pada Saluran Transmisi Tegangan Tinggi 150 kV Gardu Induk Tambak Lorok – Bawen dengan menggunakan Etap 12.6.0”. Universitas Islam Sultan Agung.

Watkins, P. C. (2004). Gratitude and Subjective Well-Being. In R. A. Emmons & M. E. McCullough (Eds.), The psychology of gratitude (pp. 167–192). Oxford University Press. https://doi.org/10.1093

/acprof:oso/9780195150100.003.0009

A. Supriyadi. 2018. “Analisa Aliran Daya Pada Sistem Tenaga Listrik Menggunakan Software ETAP 12.6,” Forum Teknologi, vol. 6, no. 3, pp. 56–65.

PT PLN (Persero), Buku 5 Standar Konstruksi Jaringan Tegangan Menengah Tenaga Listrik, Jakarta Selatan: PT PLN (Persero), 2010.

PERMEN ESDM RI No 20 Tahun 2020.”Aturan Jaringan Sistem Tenaga Listrik (Grid Code)”

PT PLN (Persero), SPLN 59:1985, Jakarta: PT PLN (Persero), Tahun 1985.

Permana, Alif. Dari: https://www.alif

pustaka.com/pengenalan-software-etap/. Diakses tanggal 18 September 2022.

PT PLN (Persero), Buku 1 Kriteria Desain Enjinering Kontruksi Jaringan Distribusi Tenaga Listrik, Jakarta Selatan: PT PLN (Persero), 2010.

Downloads

Published

2023-08-09

How to Cite

MUHAMMAD, Y. N., Darmawan, I., Andriani, T., & Hidayatullah, M. (2023). REPAIR OF KARUMBU VOLTAGE USING THE METHOD BREAKING LOAD AT PT. PLN (PERSERO) ULP WOHA. Journal Altron; Journal of Electronics, Science &Amp; Energy Systems, 2(02), 155–164. https://doi.org/10.51401/altron.v2i02.2177

Most read articles by the same author(s)

1 2 3 4 5 > >>